Hi, an update...............
Apologies it's a bit long
As mentioned I finally took the car down to 9e for my boost issues to be investigated.
Story in a nut shell.....
Car purchased from well known indy 2015, very pleased with it certainly a step up performance wise from my 996 C4S.
Car maintained by another well known indy closer to where I live. At service time May 2016, I enquired about 'pepping' her up a bit, a plan was hatched to fit GT2RS intercoolers, IPD plenum(with 82mm TB) and Y-Pipe and Kline exhaust with 100 cell cats all brought together with a custom map.
I was very pleased with the work that was done the mapping company they identified an issue with the passenger side actuator which they fixed - should really been spotted by the indy that fitted the hardware, (anyway after the work car was certainly a lot quicker – I now appreciate this is not the be all and end all :? ), and I ran the car for about a year with no issues until this April.
Then as documented at the start of this thread I lost boost, as it happened I was near the people that had performed the custom map, so I popped around (to be fair they did have a look but stressed it would have to be a quick look as they were very busy) on inspection nothing was obvious, they thought it might be the actuators or turbo
, anyway they couldn't fix it and as I was 50 miles from home I limped back.
The following week the indy that had performed the hardware install had a quick look one lunchtime, again they couldn't see anything obvious.
They couldn't book me in for 5 weeks....... (I was bit disappointed they couldn't expedite my case – they had looked after my 911's for 12 years - but fair enough).
I wasn't happy with waiting that long and I'd heard good things about 9 excellence and booked it in there for 4 weeks hence......
All I can say is wow what an operation, unlike any garage experience I have ever had...and that is in a good way I hasten to add!
From dropping off, when we sat down to discuss what the issues were and where I wanted the car to be, through to the regular updates of what was found and then next steps to discuss what options there were available etc...
After the initial chat with Ken I left feeling reassured the car was in good hands, they even managed to get the car on the ramps while I was still there to have a quick check. (Unfortunately nothing obvious).
9e are a bit of a distance from me but actually letting the train take the strain, the drop off was remarkably simple. Ken gave me a lift to the airport in the 9e Red Cayman (just back from testing and wow!), and from there the Gatwick express gets me home so quite painless and her indoors didn't have to get involved in car drop off (always a bonus!).
Anyway that afternoon I got a call from Ken detailing where they were up to with the investigation and what they'd found so far.
And.............drum roll..............the Cause of the loss of boost was one of the hoses at the back of the plenum had popped off, and driver side actuator was kaput. (To be fair the hose at the back of the plenum isn't easy to see - perhaps impossible without dropping the engine an inch or two so I can understand why it hadn't been spotted before – though the reason it had popped off was poor initial install :x
Relieved it wasn't the turbo's – phew bullet dodged........
I was a bit disappointed the original indy and the original mapper hadn't run an actuator test, which would have identified the broken actuator (it moved OK if you manually pushed it).
Anyway c'est la vie with the pipe to the plenum properly installed and a new actuator the car would be ready for road testing the following day.
Next day... and another issue... this time arguably more serious, post road test Ken gave me a call and we went over the logs.
it was explained really clearly, you could see the previous map was a bit of a mess, the ECU was compensating for the bad map , pulling timing and the Air Fuel Ratio was all over the place.
We discussed options, I wasn't prepared to keep the previous map on the car, so it was really a case of reverting to stock, which would mean removing all the performance mods or keeping the mods and getting it re-mapped by Ken, for me a no brainer.
Anyway fast forward and a couple of days later, and after several updates, the new map was on the car and Ken was happy with the map and the data that was being logged, AFR within Porsche tolerances, no horrible retardation of timing at WOT etc.....
Now it feels stock smooth bumbling around, boost comes on from really low down and boosts almost linearly, almost feels like a NA car but so so strong.
The previous map was brutal, boost used to come in with a thud, fortunately in the UK we can't sustain high speeds at boost, but I am convinced that had I had an opportunity on an Autobahn to keep 'it planted' for a sustained period I would have damaged the car.
I picked the car up at the 9e Coffee and Cars the other weekend, and at long last 2 years into Turbo ownership I finally have the car I thought the 997 Turbo was going to be from day one.
A big thank you to the team at 9e :thumbs: